Cable bead and method for manufacturing same
A manufacturing method and cable tire technology, which is applied in the field of cable bead and its manufacturing, can solve the problems of increasing the number of winding times of thin-diameter wires and consuming manufacturing time, and achieve the effect of not being easy to twist unevenly and shortening the manufacturing time
- Summary
- Abstract
- Description
- Claims
- Application Information
AI Technical Summary
Problems solved by technology
Method used
Image
Examples
Embodiment 6-1
[0171] 1×3×2.10 coreless cable bead
[0172] (Making of strand material)
[0173] A base wire obtained by drawing a brass-plated steel wire with a diameter of 6.5 mm and containing 0.7% by mass of C to a diameter of 2.10 mm was wound on three bobbins. These base wires were stranded with S strands at a stranding pitch of 50.0 mm after adjusting the diameter forming ratio to 95% using a tubular stranding machine, and were wound on a winding bobbin to produce a raw wire.
[0174] Each strand material is pulled out from the winding bobbin on which the raw wire was wound, and the end is manually untwisted, and each strand material is guided to the bobbin through a panel. use Figure 5 The shown untwisting device winds the coiled strand material on the spool, thereby obtaining 3 strand materials for the bead of the coreless cable.
[0175] (Manufacturing of coreless cable bead)
[0176] Use 1 of the 3 strand materials obtained by untwisting and winding the original wire. use ...
Embodiment 7-1
[0178] 3×2×1.48 coreless cable bead
[0179] (Making of strand material)
[0180] A base wire obtained by drawing a brass-plated steel wire with a diameter of 5.0 mm and containing 0.7% by mass of C to a diameter of 1.48 mm was wound on two bobbins. These base wires were twisted at a twisting pitch of 30 mm and Z-twisting after adjusting the diameter forming rate to 95% using a tubular stranding machine.
[0181] Then, the primary twisted material (1×2×1.48) was wound on three spools with a predetermined amount, and the diameter forming ratio was adjusted to 92% by using the tubular stranding machine again, and twisted in S at a twisting pitch of 70 mm. Retwisting is performed, and the raw wire is wound on a bobbin to produce a raw wire.
[0182] Each strand material is pulled out from the winding bobbin on which the raw wire was wound, and the end is manually untwisted, and each strand material is guided to the bobbin through a panel. use Figure 5 The shown untwisting d...
Embodiment 8-1
[0186] 3×3×1.2 coreless cable bead
[0187] (Making of strand material)
[0188] A base wire obtained by drawing a brass-plated steel wire with a diameter of 4.5 mm containing 0.7% by mass of C (carbon) to a diameter of 1.20 mm was wound on three bobbins. These base wires were twisted at a twisting pitch of 25 mm and Z-twisting after adjusting the diameter forming rate to 92% using a tubular stranding machine.
[0189] Then, the primary twisted material (1×3×1.20) was wound on three spools in a predetermined amount, and the diameter forming rate was adjusted to 99% by using the tubular stranding machine again, and twisted in S at a twisting pitch of 60 mm. Retwisting is performed, and the raw wire is wound on a bobbin to produce a raw wire.
[0190] Each strand material is pulled out from the winding bobbin on which the raw wire was wound, and the end is manually untwisted, and each strand material is guided to the bobbin through a panel. use Figure 5 The shown untwistin...
PUM
Login to View More Abstract
Description
Claims
Application Information
Login to View More 


