Production process of piston rod wire rod for vehicle
A production process and piston rod technology, which is applied in the production process of piston rod and wire rod for automobiles, can solve problems such as insufficient fatigue cycles, achieve the effect of ensuring surface quality, good dimensional accuracy, and improving decarburization control level
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Embodiment 1
[0019] A production process for piston rod wire rods for automobiles, through two-fire blanking, low-temperature rolling, low-temperature final rolling, long-term soaking, and rapid cooling to effectively control the uniformity of the grain size of the material and the depth of the decarburization layer, The C content of the piston rod wire rod for automobile is between 0.42% and 0.48%. Table 1 shows a production process control scheme for a wire rod for automobiles in Example 1. Keep the final rolling temperature below 900°C and the coiling temperature at 860°C, while the heating furnace temperature is lowered from the original 1100°C to 980°C, and the steel temperature after phosphorus removal is lowered from the original 1000°C to 905°C. As shown in Table 2, the thickness of the decarburization layer before and after the test is listed. The depth of the decarburization layer after cooling is 80.94 μm, and that before cooling is 203.62 μm.
[0020] Table 1
[0021] ...
Embodiment 2
[0025] As shown in Table 3, it is a production process of piston rod wire rod for automobiles in Example 2. While maintaining the heating temperature in the control process, the final rolling temperature was lowered from the original 980°C to 900°C, and the opening of the water tank was changed from the original If the 4#, 5#, and 6# water tanks are opened at the same time, change the opening degree of the 4# water tank to 1 / 3. Taking the reference water flow rate of 200L / min as a reference, both the 5# and 6# water tanks are closed, and the curling temperature is changed from the original The 820°C increased to 860°C.
[0026] Table 4 lists the comparison before and after the test process. According to the control process, no abnormal chilling layer was found, and the grain size of the edge and core remained basically the same, and the distribution was relatively uniform, reaching 8.5 grades.
[0027] table 3
[0028] Process plan
Finishing temperature (℃)
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